Showing posts with label rudder. Show all posts
Showing posts with label rudder. Show all posts

Tuesday, January 13, 2015

Creating the Right Tool for the Job

My father encouraged me to always use the right tool for the job.  But what do you do when there is no such tool?  Well, then you make one.  At least that's what Jeff on s/v Pilgrim does.

(Jeff and Anne are completely reconstructing Pilgrim, virtually from the hull out - most of their work is far too extensive to include here, but I encourage you to visit their website to see it.)
Any wrench large enough to fit the packing nut on Pilgrim’s possessed a handle too long to fit into the tight confines of the hull.

Looking down the rudder shaft at the packing nut.

Deep gouges along the upper edge of the nut indicated a hammer and cold chisel were used to tighten the nut.  Curiously no such evidence of similarly brutal tactics use to loosen the nut are evident.  Could it be that Pilgrim’s rudder packing is original?

Rather than attack the nut with hammer and chisel, I elected to create the proper tool for the job.

Creating a plywood template of the ideal tool for the job.

Using 1/8” luan plywood and some trial and error I created a pattern for the ideal M382 rudder post packing nut wrench.  Once satisfied with the design, I transferred the pattern to a fresh piece of plywood

Transferring the rough, initial template to a fresh piece of plywood.

A query around the commercial fishing fleet portion of the boat yard yielded a free piece of sufficiently sized 3/8” steel.

Next stop Lindow’s Machine Shop on Hwy 70 outside of Beaufort, NC.  Yup that is right... a straight up plug for Lindow’s.  Fred Lindow, owner and sole employee, has many years of personal experience on sailboats.  He does excellent work at reasonable prices.  Fred transferred the template to the metal, and then used a band saw to cut out the wrench.

Wrench clamped in vice while I clean up the rough edges with a file.

Back at the boat yard, I cleaned up the sharp edges with a file and applied a few coats of red paint.

Ready to remove the nut.

Now possessing the right tool for the job it is time to remove the packing nut.

Happiness is having the right tools for the job.

The short wrench handle and awkward body position limited the torque I could physically apply to the nut.  Ultimately removing the nut did require striking the handle of the wrench with a mallet -far preferable to further damaging the nut with blows from a cold chisel.

Removing the old packing material.

Using a combination of picks and a small flat screw driver, I excavated decaying, flax packing from the nut.  Based on the condition of the packing material I would not be surprised if it is from the original 1979 construction.  I have little doubt it was leaking when submerged.

Close up of gouges along the upper edge of Pilgrim's rudder packing nut.

A few minutes with the bench grinder’s wire wheel and the packing nut cleaned up nicely.  Despite the deep gouges along the upper edge, I do believe it remains serviceable.

Next step is to lift the boat high enough for the rudder post to clear the hull.  Hmm – I wonder how much that rudder weighs?

Our Rudder Repairs and Modifications Photo Album contains additional images and notes from this ongoing project.

Thursday, December 11, 2014

Tiller Conversion

Over on s/v Suppose, Walt & Kathy take an unusual step... And in the process demonstrate some nice prototyping skills:
Suppose, suppose... Suppose we had a tiller instead of a wheel in our boat. Wouldn't the cockpit be much more spacious, wouldn't the mechanical complexity be much less and the reliability much greater, wouldn't it be easier to feel the boat and balance the sails, and wouldn't a wind vane be much more effective. All good reasons but when we suggested the conversion to most of our sailing friends, they thought we were nuts.

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Tuesday, July 17, 2012

Rudder work

Mike of s/v Chalice takes us thru the removal of his rudder in order to replace his shaft.  This is seen by most as a daunting task, but Mike makes it sound easy (for his boat, at least):

When installing the engine, I needed to replace the old prop shaft with a longer one. I had anticipated this and had a replacement one on hand. Even though there appears to be a cutout in the rudder where it looks as though the shaft will slide in with out removing the rudder, it will not slide past. So, I had the remove the rudder. Not near as hard as I imagined it would be.

If you have to do it, here is how. First remove the steering cables from quadrant, then remove quadrant (4 bolts), then loosen a little the 3 bolts/screws that hold down the packing in the packing gland. On the outside place something under the rudder to keep it from falling out when you remove the rudder bottom pivot. I used a jack so I could lower it slowly out of the hole. You will not need to dig a hole under the rudder to gain room. You should have plenty of room if your boat is blocked up as normal, with about 12 inches under the rudder.

Installation is the reverse. I picked this time to replace my packing and cleanup and re-bed the lower pivot. I did not take a lot of pics of this process. It appears that the packing gland for the rudder shaft is something that was made in house by Cabo Rico. I also added a grease zerk to the lower pivot point to make it easier to re grease.





[Editor's note: I have become insanely fond of the GoreTex teflon packing. You tighten it until there are no drips when the shaft is turning. And it runs cool. If I was replacing my rudder packing today, I'd use it there too.]

Friday, December 17, 2010

Better than factory

Please welcome a new contributor, Paul from s/v Solace. Paul was dissatisfied with the original packing gland on the rudder shaft on Solace, and so he engineered an upgrade using modern materials:
The packing gland on the rudder shaft of my Hylas 44 never did prevent water from coming into the boat; with rate of about a drop every 10 seconds, I wanted something drier; like no water ingress.

First I removed the rudder quadrant to access the packing gland flange and cleaned up both the removable flange, (top left in photo below) and the area to be resealed (left).


I obtained a double lipped seal with stainless steel spring for my shaft which was 2.25 inches. Measuring the flange which used to press down on the packing gland, (and now inverting that flange) the sleeve measured three inches. So a seal of 2.25 ID and 3.00 OD would do it. Then I obtained a reinforced hose of 3.00 ID. I used a silicone hose but you could use a good quality rubber hose.
Next, some hose clips and gasket maker and lithium grease. I used a silicone RTV type gasket maker for motor vehicles.

Having removed the packing gland material, I started to assemble my new shaft seal. I only had about 2.75 inches of shaft to work with placing the seal on and the up turned packing gland flange took most of that.

Grease down shaft &
gasket maker applied
I applied grease down the shaft where the packing gland use to sit and gasket maker to the surface of the flange where the upturned packing gland flange will bolt to.
Slid the flange over the shaft and mated the surfaces and secured with the four bolts.



As the bolts tightened the RTV squeesed out and I left this for 24 hours to set.








Grease applied before seal
After the RTV had set, the hose was placed over the flange and I applied grease to the seal and inside the hose, pushing the grease as far down as I could get it. Then I cleaned out the surface area to where the seal would sit. This is going to have some of your favorite sealant applied here for the seal. Without the sealant, the seal will tend to slip out of the hose when pressure is applied to the hose clamp.The lower hose clamp was applied and I used my RTV sealant to the OD side of the seal and the ID of the hose. I slipped in the seal to the hose and applied the hose clamp loosely and left for 24 hrs to set before tightening a little bit more.
Finally, everything was reassembled and the boat placed back in the water. I now have a very dry rudder shaft. Now, if I can just get rid of the rain water that comes down the mast.

Costs; $30 for the seal; $18 for the hose; grease and gasket maker $20. Hose clips I had already.
Finished product
Paul
s/v Solace


Nice work Paul!
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